摘要
针对新疆油田六、九区配电电网与负荷的不合理分配、配电变压器负荷率偏低、网损率不达标等现状,分别从提高变压器的负载率、运行效率、变压器优化组合配置和应用新型节能变压器等方面进行分析并提出具体改进措施。油区变压器的改造实践效果表明,相应措施均取得了可观的经济效益,达到了节能目的,对油田油区电网大规模改造和经济运行及管理具有重要意义。
In view of the status of power distribution network at No.6 and No.9 block of Xinjiang Oilfield like insensible allocation of power distribution network and load, the lower load rate of distribution transformer and the rate of net losses not reaching the stan- dard, the analysis is carried out from the following aspects such as improving the load factor, the running efficiency, and the optimiza- tion grouping allocation of transformers, and applying new types of energy-saving transformers, together with some suggestion of con- crete improving measures. The result of reform practice for oilfield transformers indicates that corresponding measures have earned re- markable economic benefits, reached the energy-saving goal, and has great significance in the large-scale reform of oilfield power network, economic operation and management.
出处
《石油工业技术监督》
2012年第6期26-30,共5页
Technology Supervision in Petroleum Industry
关键词
配变网络
配置优化
节能
power distribution network
collocation optimization
energy-saving