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渤海绥中36-1油田注水井堵塞原因分析及解堵增注试验 被引量:7

Plugging factors analysis and plugging removal test of injectors in Suizhong area, Bohai oilfield.
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摘要 分析了造成A8 井堵塞的三种主要原因,认为堵塞的原因依次是污油堵塞、固体颗粒侵入堵塞和地层出砂堵塞。在此基础上进行了冲砂洗井和化学解堵增注试验。试验结果表明:冲砂洗井能够有效地解除井筒堵塞,化学解堵剂BRJ-9604 可以有效地解除近井地带堵塞,两者增注效果都比较明显,有效期已接近1 年。研究成果对绥中36-1 油田及其它油田的注水开发有指导和参考价值。 Three kinds of main plugging factors in A8 well have been analyzed, their sequence is effluent oil plugging, solidity invasion plugging and sanding plugging. Then the sand washing and chemical clearing tests were carried out based on the research. It shows that sand washing can remove the plugging in well bore and the chemical plug removing agent, BRJ 9604, can remove the near well bore plugging, their stimulation effects of injection wells are obvious and their valid periods are about one year. The result has guiding and reference significance to Suizhong oilfield and the others.
出处 《油气采收率技术》 CSCD 1999年第4期57-61,共5页
基金 中国海洋石油总公司研究项目
关键词 油田 注水井 堵塞 解堵增注 冲砂洗井 解堵剂 Suizhong oilfield, injector, plugging, plug removal Free words: sand washing, chemical plug removing agent
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