期刊文献+

弱碱三元复合驱抽油机井化学除垢技术研究 被引量:5

Research on chemical removel scale technology in weak base ASP flooding
在线阅读 下载PDF
导出
摘要 弱碱三元复合驱抽油机井结垢造成检泵频繁,分析了油井垢样组成、形成原因、除垢剂配方及现场除垢效果。研究结果表明:垢样含碳酸盐75%以上,少量的有机物和硅酸盐,中心井结垢频繁,当聚合物浓度在1800mg·L^-1和碱浓度800mg·L^-1以上时,卡泵现象发生的频率加大。除垢剂中HF6%。10%、盐酸10%-15%、有机酸5%~8%、螯合分散剂8%~12%、表面活性剂2%-4%、缓蚀剂0.1%~0.5%,除垢率大于95%,腐蚀率小于0.15g·m^2·h^-1,现场试验成功率80%。提前除垢和井口增加循环除垢装置,可以提高除垢成功率。 The scaling problems of rod-pumping wells in weak base ASP flooding caused pump inspection pe-riod shorten. The composition and formation mechanism of scale sample in oil-wells were studied, formula of scale remover and removing effect in feildwork were also sudied in this paper. The results showed that more than 75% of the scale composition were carbonates and the rest were organics and silicates. Rod-pumping central wells scaled frequently. When the concentration of polymer and base were above 1800mg·L^-1 and 800mg·L^-1, the frequency of pump stucking increased. The formula of scale remover were HF 6%-10%, HC1 10%-15%, organic acids 5%-8%, chelate dispersing agent 8%-12%, surfactant 2%-4%, corrosion inhibitor 0.1%-0.5%. The scale removing rate was above 95%, corrosion rate was under 0.15mg·L^-1, success rate in field was 80%.
出处 《化学工程师》 CAS 2013年第5期42-43,49,共3页 Chemical Engineer
基金 黑龙江省青年科学基金项目(QC2009C13)
关键词 弱碱三元复合驱 结垢 卡泵 除垢 酸洗 weak ASP flooding scaling formation pump stucking scale removing mixed acid washing
  • 相关文献

参考文献3

二级参考文献12

  • 1Burdyn R F, Cheng H L. Rcovery by alkaline-surfactant water flood [P]. USP:4006638, 1977--01--25.
  • 2Holm L W, Robertson S D. Improved micellar--polymer flooding with high pH chemicals[C]. SPE 7583, 1978.
  • 3Wang de-min, Zhang zhen-hua, Cheng jie-cheng, et al. Pilot test of Alkaline Surfactant Polymer Flooding in Daqing Oil Field[C].SPE 36748, 1996.
  • 4Wang de-min, Cheng jie-cheng. An Alkaline-Surfactant-Polymer Field Test in a Reservoir with a Long-term 100% Water Cut[C].SPE 49018,1998.
  • 5Wang de-min, Cheng Jie-cheng, Li qun, et al. An Alkaline/Bio--surfactant/Polymer Flooding Pilot in Daqing Oil Field[C]. SPE57304, 1999.
  • 6Krumrine P H. Scale formation during alkaline flooding. JPT, 1985,20(8) :1 466-1474.
  • 7贾庆,周斌,张彦庆,刘俊德.三元复合驱硅质垢的形成机理及影响因素[J].油气田地面工程,2001,20(1):31-32. 被引量:16
  • 8程杰成,廖广志,杨振宇,李群,姚玉明,徐典平.大庆油田三元复合驱矿场试验综述[J].大庆石油地质与开发,2001,20(2):46-49. 被引量:273
  • 9陈卫东,于会宇,倪锡成.萨北油田三元复合驱防垢技术研究[J].大庆石油地质与开发,2001,20(2):89-91. 被引量:15
  • 10徐典平,薛家锋,包亚臣,张庆权,张东,赵清萍.三元复合驱油井结垢机理研究[J].大庆石油地质与开发,2001,20(2):98-100. 被引量:54

共引文献105

同被引文献25

引证文献5

二级引证文献3

相关作者

内容加载中请稍等...

相关机构

内容加载中请稍等...

相关主题

内容加载中请稍等...

浏览历史

内容加载中请稍等...
;
使用帮助 返回顶部