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利用活性初沉池改善进水水质与强化生物脱氮研究 被引量:10

Activated Primary Clarifier for Improving Wastewater Characteristic and Enhancing Biological Nitrogen Removal
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摘要 建有初沉池的污水处理厂通常都不能满足生物脱氮除磷对碳源的需求,而取消初沉池则会增加好氧池的曝气能耗并降低生物处理工艺的稳定性。利用初沉污泥发酵来增加生物可利用的碳源被证明是行之有效的方法,其中利用活性初沉池进行污泥发酵是最为简单、改造费用最低的一种发酵方式,但其发酵效果难于控制。以北京高碑店污水厂的升级改造工程为背景,开展了将普通初沉池改造成活性初沉池的生产性试验。结果表明,活性初沉池中典型的污泥层高度为0.22~0.54m,仅为普通初沉池池边水深的5%~12%;与未改造的普通初沉池相比,经改造后的活性初沉池出水VFA、SBOD5、COD、C/N、C/P值分别增加了48.8%、45.3%、20.5%、66.2%、26.2%;活性初沉池系列的缺氧反硝化效果明显好于普通初沉池系列的,缺氧末端的硝酸盐氮浓度均值分别为3.4和8.9mg/L。因此,将普通初沉池改造成活性初沉池是实现节能降耗和稳定达标的有效措施。 WWTP with conventional primary clarifier (CPC) often can not meet the requirement for carbon source in biological nutrient removal. Moreover, the cancellation of CPC can increase the aeration energy consumption and decrease the biological treatment process stability. The primary sludge fermentation is one of the effective ways to increase carbon source, of which fermentation in activated primary clarifier (APC) is one of the simplest and lowest reconstruction cost methods. However, the shortcoming of APC is difficult to control the fermentation performance. Based on Beijing Gaobeidian WWTP upgrade project, a full-scale test was conducted by reconstructing CPC into APC. The results show that a typical sludge blanket height in APC is in range of 0.22 to 0.54 m, accounting for only 5% to 12% of the side water height in CPC. The values of VFA, SBODs, COD, C/N, C/P in the effluent of APC are 48.8% , 45.3% , 20.5% , 66.2% and 26.2% respectively higher than those in the effluent of CPC. The denitrifieation performance in APC (3.4 mg/L NO3^- -N in the end of anoxic zone) is obviously better than that in CPC (8.9 mg/L NO3^- - N in the end of anoxic zone). Therefore, reconstructing CPC into APC is one of effective measures for energy saving and stable biological nutrient removal.
出处 《中国给水排水》 CAS CSCD 北大核心 2010年第23期1-5,9,共6页 China Water & Wastewater
基金 国家水体污染控制与治理科技重大专项(2008ZX07314-008)
关键词 活性初沉池 污泥层高度 污泥发酵 生物脱氮 节能降耗 activated primary clarifier (APC) sludge blanket height sludge fermentation biological nitrogen removal energy saving and consumption reduction
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参考文献18

  • 1Smith B R. Re-thinking wastewater landscapes:Combining innovative strategies to address tomorrow' s urban wastewater treatment cha|lenges [ J ]. Water Sci Technol,2009,60(6) : 1465 - 1473.
  • 2Moser-Engleler R, Kuhni M, Bernhard C,et al. Fermentation of raw sludge on an industrial scale and applications for elutriating its dissolved products and non-sedimentable solids [ J ]. Water Res, 1999,33 ( 16 ) : 3503 - 3511.
  • 3Tchobanoglous G, Burton F L, Stensel H D. Wastewater Engineering: Treatment and Reuse [ M ]. Columbus : McGraw Hill Higher Education,2002.
  • 4Teichgraber B. Acidification of primary sludge to promote increased biological phosphorus elimination and denitrification [ J ]. Water Sci Technol, 2000,41 ( 9 ) : 163 - 170.
  • 5Andreasen K,Petersen G,Thomsen H,et al. Reduction of nutrient emission by sludge hydrolysis[ J]. Water Sci Technol, 1997,35 (10) :79 - 85.
  • 6Munch E,Koch F. A survey of prefermenter design,operation and performance in Australia and Canada [ J ]. Water Sci Technol, 1999,39 ( 6 ) : 105 - 112.
  • 7Latimer R, Pitt P, van Niekerk A. Review of primary sludge fermentation performance in South Africa and the USA [ A ]. Proceedings of the Water Environment Federation [ C ]. Alexandria: Water Environment Federation, 2007.
  • 8Chanona J,Ribes J,Sceco A,et al. Optimum design and operation of primary sludge fermentation schemes for volatile fatty acids production [ J ]. Water Res, 2006,40 ( 1 ) :53 - 60.
  • 9吕鑑,赵永志,王佳伟,周军,王洪臣,张成惠,张莉.初沉污泥水解酸化对A^2/O工艺强化除磷影响[J].北京工业大学学报,2008,34(9):981-985. 被引量:13
  • 10吴一平,王旭东.初沉污泥作为生物脱氮除磷快速碳源的转化因素研究[J].西安建筑科技大学学报(自然科学版),2005,37(4):501-503. 被引量:18

二级参考文献11

  • 1吴一平,刘莹,王旭东,彭党聪,王志盈.初沉污泥厌氧水解/酸化产物作为生物脱氮除磷系统碳源的试验研究[J].西安建筑科技大学学报(自然科学版),2004,36(4):421-423. 被引量:25
  • 2宋安宁,娄性义,韩芹.新西兰罗托鲁阿污水处理厂的处理工艺[J].中国环保产业,2005(2):42-43. 被引量:1
  • 3徐金兰 彭党聪 王志盈.关于废水生物脱氮除磷系统中的碳源问题[J].环境工程,2002,:283-283.
  • 4Banister S S,Pretorius W A. Optimisation of sludge acidogenic fermentation for biological nutrient removal[J].Water SA, 1998,24(1 ) : 35-42.
  • 5Chyi Y T,Dague R R. Effects of particulate size in anaerobic acidogenesis using cellulose as a sole carbon source [J]. Water Envir. Res,1994,66:670-678.
  • 6HENZE M, GUJER W, MINO T. Activated sludge model No.2nd, Asm 2d[J]. Water Research & Technology, 1999, 39 (1): 165-182.
  • 7ARAVINTHAN V, MINO T, TAKIZAWA S, et al. Sludge hydrolysate as a carbon source for denitrification[C] //1st World Waler Congress of the International Water Association (IWA) Conference Preprint Book3. Paris: [ s. n], 2000: 146- 153.
  • 8KARIN J. Operational factors affecting enhanced biological phosphorus removal at the waste water treatment plant in Hclsingborg[J]. War Sci Tech, 1996, 34(1/2): 67-74.
  • 9国家环保总局.水和废水分析监测方法[M].北京:中国环境科学出版社,2002.
  • 10LAHAV O, LOEWENTHAL R E. Measurement of VFA in anaerobic digestion: the five-point titration method revisited [J]. Water SA, 2000, 26(3): 389-392.

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