Injecting water into the main pipeline is a common method to prevent the ammonium salt corrosion in hydrogenation units.The use of spray nozzle can enhance the effects of washing ammonium salt and reduce the risk of a...Injecting water into the main pipeline is a common method to prevent the ammonium salt corrosion in hydrogenation units.The use of spray nozzle can enhance the effects of washing ammonium salt and reduce the risk of ammonium salt corrosion.The droplet atomization and evaporation model were used to investigate the mixing process of injecting water and gas-oil mixture in a high-pressure environment.The effects of some key parameters including fluid velocity,temperature,and droplet volume fraction on the mixing and vaporization process were analyzed.Numerical simulation results show that with the increase of injecting water flow rate,the fluid velocity increases and the temperature decreases continuously.When the mass flow rate of injecting water is 1.5 t/h,the droplet has the maximum evaporation efficiency and the volume fraction reaches a minimum value.Besides,with the increase of atomization angle and droplet size,the mean velocity and the temperature of fluid decrease continuously.The increase of atomization angle or the decrease of droplet size will accelerate the evaporation process of droplets and reduce the droplet volume fraction,which indicates that the droplet slip velocity and the contact area are the key factors affecting the droplet evaporation rate.展开更多
Objective To evaluate the performance of vaporized hydrogen peroxide (VHP) for the bio-decontamination of the high efficiency particulate air (HEPA) filter unit. Methods Self-made or commercially available bioindi...Objective To evaluate the performance of vaporized hydrogen peroxide (VHP) for the bio-decontamination of the high efficiency particulate air (HEPA) filter unit. Methods Self-made or commercially available bioindicators were placed at designated locations in the HEPA filter unit under VHP fumigation. The spores on coupons were then extracted by 0.5 h submergence in eluent followed by 200- time violent knocks. Results Due to the presence of HEPA filter in the box, spore recovery from coupons placed at the bottom of the filter downstream was significantly higher than that from coupons placed at the other locations. The gap of decontamination efficiency between the top and the bottom of the filter downstream became narrower with the exposure time extended. The decontamination efficiency of the bottom of the filter downstream only improved gently with the injection rate of H202 increased and the decontamination efficiency decreased instead when the injection rate exceeded 2.5 g/min. The commercially available bioindicators were competent to indicate the disinfection efficiency of VHP for the HEPA filter unit. Conclusion The HEPA filter unit is more difficult than common enclosure to decontaminate using VHP fumigation. Complete decontamination can be achieved by extending fumigation time. VHP fumigation can be applied for in-situ biodecontamination of the HEPA filter unit as an alternative method to formaldehyde fumigation.展开更多
Novel linear supramolecular polymers were successfully constructed by self-assemblies of coumarinbridged bifunctional UPy derivative.Benefitting from the photodimerization ability of the coumarin moieties,the linear s...Novel linear supramolecular polymers were successfully constructed by self-assemblies of coumarinbridged bifunctional UPy derivative.Benefitting from the photodimerization ability of the coumarin moieties,the linear supramolecular polymers could form the large three-dimensional polymer networks upon UV light irradiation via photo-cross-linking,which provides a viable and alternative procedure to modulate the properties of supramolecular polymers.展开更多
After having expanded its capacity from 300 kt/a to 450 kt/a in 1994, the steam cracking unit of Yanshan Petrochemical Company was still experiencing such problems as low feedstock flexibility, high energy consumption...After having expanded its capacity from 300 kt/a to 450 kt/a in 1994, the steam cracking unit of Yanshan Petrochemical Company was still experiencing such problems as low feedstock flexibility, high energy consumption and smaller production capacity as compared to other ethylene units constructed in the same time. In order to fully improve technical capability, reduce energy consumption, improve feedstock flexibility and increase production capacity of steam crackers, a lot of technical transform schemes on steam cracking were studied and compared with attention focused on the feasibility, safety, operability of the related revamp schemes, as well as the advanced nature and economical features. The transform scheme decided includes following projects. For the pyrolysis quench compression system, the pyrolysis gasoline fractionation tower is retrofitted on the site, quench water tower, pyrolysis gas compressor and steam turbine are replaced by new ones respectively. For the separation system a low pressure methane removal technology is adopted with the demethanizer tower replaced, coupled with the C 3 catalytic rectification/hydrogenation technology, while the high pressure depropanizer is replaced with addition of a propylene rectification tower. The fractionation flow sheet and equipment are adjusted with addition of a propylene compressor and compressor for binary mixture of methane ethylene cooling agents. The revamped complex has expanded the ethylene capacity to the target of 660 kt/a with the actual capacity reaching 710 kt/a, remarkably reduced the energy consumption, and is capable of using naphtha, light diesel fuel, heavy diesel fuel and the hydrocracked tail oil as the steam cracking feedstock. This project is the first to apply refrigeration by means of a mixed cooling agent and has succeeded in using C\-3 catalytic rectification/hydrogenation technology, which has given an impetus to the progress of steam cracking industry in the world.展开更多
基金The authors acknowledge supports from the National Natural Science Foundation of China(Grant No.51806198,No.U1909216,No.52176048,No.51876194)the Zhejiang Provincial Natural Science Foundation(Grant No.LY21E060011)the Fundamental Research Funds of Zhejiang Sci-Tech University(Grant No.2021Q020).
文摘Injecting water into the main pipeline is a common method to prevent the ammonium salt corrosion in hydrogenation units.The use of spray nozzle can enhance the effects of washing ammonium salt and reduce the risk of ammonium salt corrosion.The droplet atomization and evaporation model were used to investigate the mixing process of injecting water and gas-oil mixture in a high-pressure environment.The effects of some key parameters including fluid velocity,temperature,and droplet volume fraction on the mixing and vaporization process were analyzed.Numerical simulation results show that with the increase of injecting water flow rate,the fluid velocity increases and the temperature decreases continuously.When the mass flow rate of injecting water is 1.5 t/h,the droplet has the maximum evaporation efficiency and the volume fraction reaches a minimum value.Besides,with the increase of atomization angle and droplet size,the mean velocity and the temperature of fluid decrease continuously.The increase of atomization angle or the decrease of droplet size will accelerate the evaporation process of droplets and reduce the droplet volume fraction,which indicates that the droplet slip velocity and the contact area are the key factors affecting the droplet evaporation rate.
基金supported by the Research Fund from the Ministry of Science and Technology of the People’s Republic of China, 2009ZX10004-502 and 2009ZX10004-709
文摘Objective To evaluate the performance of vaporized hydrogen peroxide (VHP) for the bio-decontamination of the high efficiency particulate air (HEPA) filter unit. Methods Self-made or commercially available bioindicators were placed at designated locations in the HEPA filter unit under VHP fumigation. The spores on coupons were then extracted by 0.5 h submergence in eluent followed by 200- time violent knocks. Results Due to the presence of HEPA filter in the box, spore recovery from coupons placed at the bottom of the filter downstream was significantly higher than that from coupons placed at the other locations. The gap of decontamination efficiency between the top and the bottom of the filter downstream became narrower with the exposure time extended. The decontamination efficiency of the bottom of the filter downstream only improved gently with the injection rate of H202 increased and the decontamination efficiency decreased instead when the injection rate exceeded 2.5 g/min. The commercially available bioindicators were competent to indicate the disinfection efficiency of VHP for the HEPA filter unit. Conclusion The HEPA filter unit is more difficult than common enclosure to decontaminate using VHP fumigation. Complete decontamination can be achieved by extending fumigation time. VHP fumigation can be applied for in-situ biodecontamination of the HEPA filter unit as an alternative method to formaldehyde fumigation.
基金sponsored by National Natural Science Foundation of China(Nos.21602112 and 21472088)supported by Scientific Starting Fund from Nanjing University of Posts and Telecommunications(NUPTSF)(No.NY215057)
文摘Novel linear supramolecular polymers were successfully constructed by self-assemblies of coumarinbridged bifunctional UPy derivative.Benefitting from the photodimerization ability of the coumarin moieties,the linear supramolecular polymers could form the large three-dimensional polymer networks upon UV light irradiation via photo-cross-linking,which provides a viable and alternative procedure to modulate the properties of supramolecular polymers.
文摘After having expanded its capacity from 300 kt/a to 450 kt/a in 1994, the steam cracking unit of Yanshan Petrochemical Company was still experiencing such problems as low feedstock flexibility, high energy consumption and smaller production capacity as compared to other ethylene units constructed in the same time. In order to fully improve technical capability, reduce energy consumption, improve feedstock flexibility and increase production capacity of steam crackers, a lot of technical transform schemes on steam cracking were studied and compared with attention focused on the feasibility, safety, operability of the related revamp schemes, as well as the advanced nature and economical features. The transform scheme decided includes following projects. For the pyrolysis quench compression system, the pyrolysis gasoline fractionation tower is retrofitted on the site, quench water tower, pyrolysis gas compressor and steam turbine are replaced by new ones respectively. For the separation system a low pressure methane removal technology is adopted with the demethanizer tower replaced, coupled with the C 3 catalytic rectification/hydrogenation technology, while the high pressure depropanizer is replaced with addition of a propylene rectification tower. The fractionation flow sheet and equipment are adjusted with addition of a propylene compressor and compressor for binary mixture of methane ethylene cooling agents. The revamped complex has expanded the ethylene capacity to the target of 660 kt/a with the actual capacity reaching 710 kt/a, remarkably reduced the energy consumption, and is capable of using naphtha, light diesel fuel, heavy diesel fuel and the hydrocracked tail oil as the steam cracking feedstock. This project is the first to apply refrigeration by means of a mixed cooling agent and has succeeded in using C\-3 catalytic rectification/hydrogenation technology, which has given an impetus to the progress of steam cracking industry in the world.